I am using PID for boost control and I am getting a positive correction even though I am over the target boost.
Around 1 minute 40 seconds in the log is where I am accelerating.
Any advice you can give me?
bstv13.emub3 (67.6 KB)
bstv13.emublog3 (1.1 MB)
Please go to Other/PID monitor and select Boost there will be additional debug of PID controller. It looks like your I term is very small. Your boost margin is quite big and it looks like I term rises and then the error is very small and it drops down very very slow.
You can also try defualt pid settings.
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